[1]殷立洪.某G105钻杆接头损坏原因分析[J].焊管,2016,39(9):54-58.[doi:10.19291/j.cnki.1001-3938.2016.09.012]
 YIN Lihong,ZHANG Jun.Damage Reason Analysis of Some G105 Drill Pipe Joint[J].,2016,39(9):54-58.[doi:10.19291/j.cnki.1001-3938.2016.09.012]
点击复制

某G105钻杆接头损坏原因分析
分享到:

《焊管》[ISSN:1001-3938/CN:61-1160/TE]

卷:
39
期数:
2016年第9期
页码:
54-58
栏目:
经验交流
出版日期:
2016-09-28

文章信息/Info

Title:
Damage Reason Analysis of Some G105 Drill Pipe Joint
文章编号:
10.19291/j.cnki.1001-3938.2016.09.012
作者:
殷立洪1 2张 钧1
1. 西安石油大学 材料科学与工程学院, 西安 710065;
2. 宝鸡石油钢管有限责任公司, 陕西 宝鸡 721008
Author(s):
YIN Lihong1 2 ZHANG Jun1
1. School of Materials Science and Engineering, Xi’an Shiyou University, Xi’an 710065, China;
2. Baoji Petroleum Steel Pipe Co., Ltd., Baoji 721008, Shaanxi, China
关键词:
钻杆接头螺纹粘着磨损
Keywords:
drill pipe joint thread adhesive wear and tear
分类号:
TE921
DOI:
10.19291/j.cnki.1001-3938.2016.09.012
文献标志码:
B
摘要:
为了找出某油田G105钻杆内、外螺纹接头损伤原因,对现场使用的失效钻杆接头进行了宏观分析、理化性能检验、金相及显微组织分析。结果表明,受损的钻杆内、外螺纹接头的化学成分和力学性能均满足API SPEC 5DP—2009标准要求,钻杆接头主要的失效原因为粘着磨损,是在上扣过程中扭矩过大造成的,同时,螺纹脂涂抹不均匀、钻杆接头镀层质量欠佳也是造成粘着磨损的因素。
Abstract:
In order to find out the damage reason of G105 drill pipe internal and external thread joint, the macro analysis, physical and chemical properties test, metallographic and microstructure analysis were carried out for the failure drill pipe joint. The results indicated that the chemical composition and mechanical properties of damaged internal and external thread joint of drill pipe can meet the requirements of API SPEC 5DP—2009 standard, the main failure reason of drill pipe joint is adhesive wear and tear, which caused by excessive torque in the process of screw on, at the same time, the uneven thread compound daub and poor quality of drill pipe joint coating both are the factors for adhesive wear and tear.

参考文献/References:

[1] 孙智,江利,应鹏展. 失效分析基础与应用[M]. 北京:机械工业出版社,2009.
[2] 王银强. 油气管线穿越钻杆失效分析及预防[D]. 西安:西安石油大学,2015.
[3] API SPEC 5DP—2009,Specification for Drill Pipe[S].
[4] 李炯辉,林德成. 金属材料金相图谱[M]. 北京:机械工业出版社,2006.
[5] 续海峰. 粘着磨损机理及其分析[J]. 机械管理开发,2007(S1):101-102,104.
[6] 马丽心,刘义翔,李文新. 粘着磨损及影响因素的研究[J]. 哈尔滨商业大学学报,2001(1):76-78.
[7] 张毅,王治国,刘甫清. 钻杆接头双台肩抗扭应力分析[J]. 钢管,2003(5):9-12.
[8] 李方坡,刘永刚,林凯,等. G105油井钻杆失效分析[J]. 金属热处理,2009,34(10):94-96.
[9] 刘志超,冯爽,姚久红,等. 钻杆的失效分析和检测现状及其研究进展[J]. 热加工工艺,2015(6):16-19.
[10] 张毅,赵仁存,张汝忻. 国内外高强度钻杆的技术质量评述[J]. 钢管,2000,29(5):1-8.

相似文献/References:

[1]徐刚,王旭,李建强,等.钻杆压接生产线搬运自动控制系统[J].焊管,2010,33(10):42.[doi:1001-3938(2010)10-0042-04]
 XU Gang,WANG Xu,LI Jian-qiang,et al.Conveying Automatic Control System of Drill Pipe Crimping Production Line[J].,2010,33(9):42.[doi:1001-3938(2010)10-0042-04]
[2]姚 欢,高惠临,巨西民,等.便携式漏磁检测系统钻杆管体检测技术研究[J].焊管,2011,34(12):32.[doi:1001-3938(2011)12-0032-04]
 YAO Huan,GAO Hui-lin,JU Xi-min,et al.Research on inspection of drill pipe body through Portable Magnetic Flux Leakage Detection System[J].,2011,34(9):32.[doi:1001-3938(2011)12-0032-04]
[3]张华佳,李 娜,范 炜,等.焊后热处理对摩擦焊钻杆性能的影响[J].焊管,2016,39(2):39.[doi:10.19291/j.cnki.1001-3938.2016.02.009]
 ZHANG Huajia,LI Na,FAN Wei,et al.Effect of the Post-weld Heat Treatment on Friction Welding Drill Pipe Properties[J].,2016,39(9):39.[doi:10.19291/j.cnki.1001-3938.2016.02.009]
[4]白 鹤,呼延辉,李 超,等.油套管接头加工质量控制方法研究[J].焊管,2018,41(8):60.[doi:10.19291/j.cnki.1001-3938.2018.08.011]
 BAI He,HU Yanhui,LI Chao,et al.Research on the Methods of Quality Control for Tubing and Casing Connection Processing[J].,2018,41(9):60.[doi:10.19291/j.cnki.1001-3938.2018.08.011]
[5]赵金兰,李京川,瞿婷婷,等.某S135钻杆管体断裂失效原因分析[J].焊管,2018,41(11):48.[doi:10.19291/j.cnki.1001-3938.2018.11.011]
 ZHAO Jinlan,LI Jingchuan,QU Tingting,et al.Fracture Failure Analysis of a S135 Drill Pipe Body[J].,2018,41(9):48.[doi:10.19291/j.cnki.1001-3938.2018.11.011]
[6]任 武,荆 栋,王海飞,等.CT90级连续油管激光焊对接接头的组织及性能研究[J].焊管,2019,42(12):23.[doi:10.19291/j.cnki.1001-3938.2019.12.005]
 REN Wu,JING Dong,WANG Haifei,et al.Research on Microstructure and Properties of Laser Welding Butt Joint for CT90 Coiled Tubing[J].,2019,42(9):23.[doi:10.19291/j.cnki.1001-3938.2019.12.005]
[7]赵金兰,李京川,王 康,等.某G105钻杆管体刺穿失效原因分析[J].焊管,2020,43(11):36.
 ZHAO Jinlan,LI Jingchuan,WANG Kang,et al.Causes Analysis of a G105 Drill Pipe Body Piecing Failure[J].,2020,43(9):36.
[8]赵金兰,王 焘,王玉成,等.S135钻杆管体到加厚过渡段区域失效分析[J].焊管,2021,44(1):32.[doi:10.19291/j.cnki.1001-3938.2021.01.006]
 ZHAO Jinlan,WANG Dao,WANG Yucheng,et al.Failure Analysis of S135 Drill Pipe Transition Section from Pipe Body to Thickening[J].,2021,44(9):32.[doi:10.19291/j.cnki.1001-3938.2021.01.006]
[9]王显林,陈长青,韩 旭,等.摩擦焊接式全钛合金钻杆焊区性能评价与研究[J].焊管,2021,44(5):19.[doi:10.19291/j.cnki.1001-3938.2021.05.004]
 WANG Xianlin,CHEN Changqing,HAN Xu,et al.Performance Evaluation and Research of Weld Zone for Friction Welded All Titanium Alloy Drill Pipe[J].,2021,44(9):19.[doi:10.19291/j.cnki.1001-3938.2021.05.004]
[10]赵金兰,曾红伟,李京川,等.某 S135 钻杆接头刺漏原因分析[J].焊管,2021,44(5):44.[doi:10.19291/j.cnki.1001-3938.2021.05.008]
 ZHAO Jinlan,ZENG Hongwei,LI Jingchuan,et al.Cause Analysis on Leakage of a S135 Drill Pipe Joint[J].,2021,44(9):44.[doi:10.19291/j.cnki.1001-3938.2021.05.008]

备注/Memo

备注/Memo:
收稿日期: 2016-08-06
作者简介:  殷立洪(1972—),男,高级工程师,西安石油大学在读硕士研究生,长期从事焊管生产管理工作。
更新日期/Last Update: