[1]杨宏利,王 军.30CrMoA抽油杆失效分析[J].焊管,2017,40(7):64-68.[doi:10.19291/j.cnki.1001-3938.2017.07.012]
 YANG Hongli,WANG Jun.Failure Analysis of the 30CrMoA Sucker Rod[J].,2017,40(7):64-68.[doi:10.19291/j.cnki.1001-3938.2017.07.012]
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30CrMoA抽油杆失效分析
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《焊管》[ISSN:1001-3938/CN:61-1160/TE]

卷:
40
期数:
2017年第7期
页码:
64-68
栏目:
经验交流
出版日期:
2017-07-28

文章信息/Info

Title:
Failure Analysis of the 30CrMoA Sucker Rod
文章编号:
10.19291/j.cnki.1001-3938.2017.07.012
作者:
杨宏利王 军
西安三维应力工程技术有限公司, 西安 710061
Author(s):
YANG Hongli WANG Jun
Xi’an Serv Stress Engineering Technology Co., Ltd., Xi’an 710061, China
关键词:
抽油杆机械损伤疲劳失效过程检测
Keywords:
sucker rod mechanical damage fatigue failure process detection
分类号:
TE933.2
DOI:
10.19291/j.cnki.1001-3938.2017.07.012
文献标志码:
B
摘要:
为了研究抽油杆的失效原因和减少抽油杆的断井事故,对现场取回的抽油杆失效样品进行几何尺寸测量和理化性能检测,并对断口进行宏观、微观分析及载荷分析。检测及分析结果显示,抽油杆几何尺寸、理化性能符合相关标准要求,满足其使用性能要求;断口起源于机械损伤部位,随着周期性的载荷作用,疲劳损伤不断积累,最终导致抽油杆扳手方发生疲劳断裂,裂纹宏观及微观均呈现疲劳裂纹扩展特征。失效分析结果表明,要保证抽油杆的使用安全,除产品质量这一重要因素外,对抽油杆的使用过程进行监测控制也是很重要的环节。
Abstract:
In order to study the failure cause of the sucker rod and reduce the breaking off accident of sucker rod in the well. The sucker rod failure sample was retrieved from the job site, the geometry size of sample was measured, the physical and chemical properties of sample were tested, and the macro and micro analysis, load analysis of sample fracture were finished. After the testing and analysis, the results indicated that the geometry size, physical and chemical properties of the sucker rod meet the requirements of the relevant standards and meet usage performance equirements; the sample fracture originated from the mechanical damage,with periodic loading, the fatigue damage was accumulated, which caused a fatigue fracture of the sucker rod wrench eventually, both macro and micro crack showed fatigue crack propagation characteristic. According to the failure analysis results, in order to ensure the safety of using the sucker rod, monitoring and controlling the using process of the sucker rod is an important factor besides the product quality.

参考文献/References:

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备注/Memo

备注/Memo:
收稿日期:2017-04-17
作者简介:杨宏利(1984—),本科,助理工程师,目前主要从事石油管材检测及失效分析工作。
更新日期/Last Update: