[1]鲁明春.水平井连续管存储式测井技术在涩北气田的试验应用[J].焊管,2014,37(11):27-29.[doi:1001-3938(2014)11-0027-03]
 LU Mingchun.Test Application of Horizontal Coiled Tubing Store Type Logging Technology in China Sebei Gas Field[J].,2014,37(11):27-29.[doi:1001-3938(2014)11-0027-03]
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水平井连续管存储式测井技术在涩北气田的试验应用
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《焊管》[ISSN:1001-3938/CN:61-1160/TE]

卷:
37
期数:
2014年第11期
页码:
27-29
栏目:
应用与开发
出版日期:
2014-11-28

文章信息/Info

Title:
Test Application of Horizontal Coiled Tubing Store Type
Logging Technology in China Sebei Gas Field
文章编号:
1001-3938(2014)11-0027-03
作者:
鲁明春
(青海油田井下作业公司,青海 茫崖817500)
Author(s):
LU Mingchun
(Qinghai Oilfield Downhole Operation Company,Mangya 817500,Qinghai,China)
关键词:
连续管涩北气田存储式测井近平衡作业
Keywords:
coiled tubingChina Sebei gas field store type loggingnearly balance operation
分类号:
TG973
DOI:
1001-3938(2014)11-0027-03
文献标志码:
B
摘要:
涩北气田因储层出砂十分严重,水平井采用常规电缆生产测井成功率低,成本高,且存在风险。在此背景下,引进了连续管存储式测井技术,该技术可实现不动管柱带压冲砂和生产测井一体化作业,可最大限度地缩短停产作业时间,降低了仪器砂卡的风险。连续管存储式测井技术经过4口井的现场试验,应用结果表明,连续管存储式测井技术成功解决了涩北气田水平井生产测井仪器输送和砂卡的技术难题,实现了安全、高效、低成本作业,同时还具有安全环保的优势。
Abstract:
In China Sebei gas field, the sands flowing from store layer is serious, adopting the conventional cable to conduct production logging in horizontal well, the success rate is low, high cost and exist risk. Under this background, the coiled tubing store type logging technology was introduced;this technology can realize sands washing with pressure without pulling string and integration of production logging operations, which can shorten the shutdown operation time at utmost, reduce the risk of sand sticking. After field test in four wells for the above technology, the application results indicated that the coiled tubing store type logging technology successfully solved the technological problem of logging instrument delivery and sand sticking, and realized safe and high efficiency production with low cost, and with the advantage of safety and environmental protection.

参考文献/References:

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备注/Memo

备注/Memo:
收稿日期:2014-04-01
作者简介:鲁明春(1968—),男,高级工程师,主要从事石油地质的勘探与开发工作。
更新日期/Last Update: